NTSB: NWA Flight 74 Crew Thought Gear Was Down | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.29.24

Airborne-NextGen-04.30.24

Airborne-Unlimited-05.01.24 Airborne-AffordableFlyers--05.02.24

Airborne-Unlimited-05.03.24

Mon, Dec 22, 2008

NTSB: NWA Flight 74 Crew Thought Gear Was Down

Faulty Nose Gear Door Actuator Examined

The National Transportation Safety Board has released an updated factual report on the Northwest Airlines Flight 74 landing accident at Guam International Airport (GUM) on August 19, 2005.

As ANN reported, the NWA Boeing 747-200 experienced trouble extending the landing gear on approach to GUM, indicated by a red light on the landing gear indicator and a warning horn. After aborting the initial approach and consulting a cockpit operations manual, the flight crew concluded the landing gear was "down and locked."

Soon after touchdown, the nose gear collapsed, and the plane skidded to a stop on the runway. The 340 persons aboard evacuated the stricken jet via inflatable slides, with only two minor injuries reported. The aircraft, damaged beyond all repair, was eventually scrapped, the Guam Pacific Daily News said.

Subsequent examination and testing of the aircraft's nose gear components revealed several problems with the landing gear door actuator: one of two "lock keys" was found to be installed backward; strands of metallic material were found in different areas of the actuator; the "manual override crank gland was found lightly torqued with safety wire installed"; the "lock ram and lock ring" were damaged; and the piston rod seal was "installed with non-standard backup rings," according to the report.

Unknown to the flight crew of Flight 74, the same aircraft had experienced similar problems just 10 days prior, but the captain of that flight failed to make note of it in the plane's maintenance log.

The NTSB's final report on the accident and determination of probable cause has not yet been released.

FMI: www.nwa.com, www.ntsb.org

Advertisement

More News

ANN's Daily Aero-Term (04.30.24): Runway Centerline Lighting

Runway Centerline Lighting Flush centerline lights spaced at 50-foot intervals beginning 75 feet from the landing threshold and extending to within 75 feet of the opposite end of t>[...]

ANN's Daily Aero-Linx (04.30.24)

Aero Linx: Air Force Global Strike Command Air Force Global Strike Command, activated August 7, 2009, is a major command with headquarters at Barksdale Air Force Base, Louisiana, i>[...]

Airborne 04.24.24: INTEGRAL E, Elixir USA, M700 RVSM

Also: Viasat-uAvionix, UL94 Fuel Investigation, AF Materiel Command, NTSB Safety Alert Norges Luftsportforbund chose Aura Aero's little 2-seater in electric trim for their next gli>[...]

Airborne 04.29.24: EAA B-25 Rides, Textron 2024, G700 Deliveries

Also: USCG Retires MH-65 Dolphins, Irish Aviation Authority, NATCA Warns FAA, Diamond DA42 AD This summer, history enthusiasts will have a unique opportunity to experience World Wa>[...]

Airborne-NextGen 04.23.24: UAVOS UVH 170, magni650 Engine, World eVTOL Directory

Also: Moya Delivery Drone, USMC Drone Pilot, Inversion RAY Reentry Vehicle, RapidFlight UAVOS has recently achieved a significant milestone in public safety and emergency services >[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC