NTSB Continues Investigation Of Dreamliner Engine Failure In SC | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.22.24

Airborne-Unlimited-04.16.24

Airborne-FlightTraining-04.17.24 Airborne-AffordableFlyers-04.18.24

Airborne-Unlimited-04.19.24

Join Us At 0900ET, Friday, 4/10, for the LIVE Morning Brief.
Watch It LIVE at
www.airborne-live.net

Fri, Sep 28, 2012

NTSB Continues Investigation Of Dreamliner Engine Failure In SC

Reports That A Second Cracked Fan Midshaft Was Discovered In A GEnx-1B Engine On A 787 Which Had Not Yet Flown

The NTSB is continuing its investigation of an incident which occurred on July 28, 2012 involving a Boeing 787-8 airplane that experienced a loss of thrust in the right engine—a General Electric (GE) GEnx-1B turbofan – during a pre-first flight, low-speed taxi test at Charleston International Airport in Charleston, South Carolina. As reported in an earlier update, the investigation found that the forward end of the fan midshaft (FMS) fractured and separated. Examination of other pre-delivery engines revealed a second GEnx-1B engine with a cracked FMS that was installed on a 787-8 airplane that had not yet flown.

The investigation is ongoing, and an initial inspection of all in-service GEnx engines has been completed. Most recently, on September 11, 2012, a Boeing 747-8F with GE GEnx-2B turbofan engines experienced a loss of power in the No. 1 engine during the takeoff roll at Shanghai Pudong International Airport, Shanghai, China. The Civil Aviation Administration of China (CAAC) is investigating this incident, and the NTSB is participating as the state of design and manufacture of the engine and aircraft. Any investigative updates regarding this incident will be provided by the CAAC.

As part the CAAC’s investigation and in relation to the NTSB’s ongoing investigation of the July 28th engine failure, preliminary findings from the examination of the Shanghai incident engine revealed that the FMS was intact and showed no indications of cracking. The examination and teardown of that engine is continuing under the direction of the CAAC.

FMI: www.ntsb.gov

 


Advertisement

More News

ANN's Daily Aero-Term (04.24.24): Runway Lead-in Light System

Runway Lead-in Light System Runway Lead-in Light System Consists of one or more series of flashing lights installed at or near ground level that provides positive visual guidance a>[...]

ANN's Daily Aero-Linx (04.24.24)

Aero Linx: Aviation Without Borders Aviation Without Borders uses its aviation expertise, contacts and partnerships to enable support for children and their families – at hom>[...]

Aero-FAQ: Dave Juwel's Aviation Marketing Stories -- ITBOA BNITBOB

Dave Juwel's Aviation Marketing Stories ITBOA BNITBOB ... what does that mean? It's not gibberish, it's a lengthy acronym for "In The Business Of Aviation ... But Not In The Busine>[...]

Classic Aero-TV: Best Seat in The House -- 'Inside' The AeroShell Aerobatic Team

From 2010 (YouTube Version): Yeah.... This IS A Really Cool Job When ANN's Nathan Cremisino took over the lead of our Aero-TV teams, he knew he was in for some extra work and a lot>[...]

Airborne Affordable Flyers 04.18.24: CarbonCub UL, Fisher, Affordable Flyer Expo

Also: Junkers A50 Heritage, Montaer Grows, Dynon-Advance Flight Systems, Vans' Latest Officially, the Carbon Cub UL and Rotax 916 iS is now in its 'market survey development phase'>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC