Five Years Later, What Happened To Payne Stewart? | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.29.24

Airborne-NextGen-04.30.24

Airborne-Unlimited-05.01.24 Airborne-AffordableFlyers--05.02.24

Airborne-Unlimited-05.03.24

Tue, Oct 26, 2004

Five Years Later, What Happened To Payne Stewart?

And Still, Virtually No Answers

It was a somber anniversary Monday for both the world of golf and the world of aviation. Five years ago, golfer Payne Stewart and five others were killed in a bizarre accident involving a Lear 35. Investigators believe that the aircraft lost cabin pressure shortly after taking off from Orlando (FL), headed to Dallas (TX). But, ultimately, what caused the loss of cabin pressure remains just as much a mystery as it was five years ago.

The End Of N47BA

The accident aircraft, N47BA, was owned by Sunjet Aviation, an on-demand air taxi operation based

Instead of landing in Dallas, the Lear 35 continued flying at altitude for four hours, a ghost ship with no one at the controls. The aircraft was intercepted twice -- first, by F-16s with the Oklahoma Air Guard, and then by a pair of Falcons from the North Dakota Air Guard. Finally, near Aberdeen (SD), the Lear's fuel supply was exhausted. The Lear lost power and spiraled into the ground.

The NTSB final report on the accident was released November 28th, 2000, more than a year later. In it, investigators listed the probable cause as "incapacitation of the flight crew members as a result of their failure to receive supplemental oxygen following a loss of cabin pressurization, for undetermined reasons."

History Of Pressurization Trouble

N47BA wasn't the first choice for Stewart's last flight. The 42-year old golfer and his three companions were to have taken a commercial flight from Orlando to Dallas. But fellow golfers Van Arden and Robert Fraley convinced Stewart that flying an air taxi was safer. Even though Stewart himself owned a piece of an aircraft, the tab for this ride was being picked up by a sponsor.

The aircraft had just come out of the shop, according to published reports. Pilots on recent flights had reported problems with the cabin pressurization, saying it sometimes failed to hold pressure at lower altitudes. A maintenance supervisor at Sunjet told investigators that, prior to its last flight, N47BA was being checked for a 'throttle problem.' During a visual inspection of the left engine, the supervisor spotted a problem with an engine modulation valve. He said "the spring [was] not functioning." The valve was replaced the next day.

The repair tag on the old valve read, "Reason removed: ITT (interstage turbine temperature) split at altitude and cabin pressurization loss with reduced power setting."

Sunjet executives said the aircraft was flown once before it was put back into service. However, investigators found that, during the test flight, the aircraft never flew above 13,000 feet.

The replacement valve was never officially blamed for the depressurization that led to the accident. But the NTSB report noted that it had been the object of scrutiny as early as four years before the crash.

On April 12, 1995, a prepurchase inspection performed by Learjet at its Wichita (KS), facility indicated the following:

Cabin pressure follows throttles - 2,000 feet bump both directions...R/H [right] engine mod...Valve does not shift when power is brought up...when moving cabin air switch to max flow you get no increase of air flow...with cabin pressure at 1 pound in auto, cabin will not up rate when selecting a higher altitude...should up rate depending on where rate knob is at...emergency exit seal...coming loose...main cabin door is smashed at split line area...O2 need serviced.

Investigators did find the valves in the wreckage of N47BA and noted, "On October 23, 1999, the left engine modulation valve, S/N P-247, was removed and replaced with one of the modulation valves that was discovered in the wreckage. The functional test of the replaced modulation valve revealed that the flow mixing poppet between the low- and high-pressure stages did not operate (open) at low bleed air pressures."

FMI: www.ntsb.gov

Advertisement

More News

ANN's Daily Aero-Term (05.01.24): Say Altitude

Say Altitude Used by ATC to ascertain an aircraft's specific altitude/flight level. When the aircraft is climbing or descending, the pilot should state the indicated altitude round>[...]

ANN's Daily Aero-Linx (05.01.24)

Aero Linx: European Air Law Association (EALA) EALA was established in 1988 with the aim to promote the study of European air law and to provide an open forum for those with an int>[...]

Classic Aero-TV: Korean War Hero Twice Reborn

From 2023 (YouTube Version): The Life, Death, Life, Death, and Life of a Glorious Warbird In 1981, business-owner Jim Tobul and his father purchased a Chance-Vought F4U Corsair. Mo>[...]

Airborne 04.29.24: EAA B-25 Rides, Textron 2024, G700 Deliveries

Also: USCG Retires MH-65 Dolphins, Irish Aviation Authority, NATCA Warns FAA, Diamond DA42 AD This summer, history enthusiasts will have a unique opportunity to experience World Wa>[...]

Airborne Affordable Flyers 05.02.24: Bobby Bailey, SPRG Report Cards, Skydive!

Also: WACO Kitchen Bails, French SportPlane Mfr to FL, Dynon-Advance Flight Systems, Innovation Preview Bobby Bailey, a bit of a fixture in sport aviation circles for his work with>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC