Report: China Airlines 747-200 Had Bad Repair | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-05.06.24

Airborne-NextGen-04.30.24

Airborne-Unlimited-05.01.24 Airborne-AffordableFlyers--05.02.24

Airborne-Unlimited-05.03.24

Wed, Jun 04, 2003

Report: China Airlines 747-200 Had Bad Repair

225 Died a Year Ago, on Approach to Taiwan's Penghu Island

China Airlines Flight CI611 made headlines a year ago, May, when it inexplicably disappeared from radar. 225 people were killed, including 19 crew; and recovery efforts were hampered by rough waters, for many days.

Now, some new facts are pointing to a possible cause of the disaster: investigators are pointing to an inadequate repair job performed on the then nearly-new plane in 1980. (The craft was built in 1979.)

What happened, had to do with a patch to the rear cargo door area of the fuselage. That area had been damaged by a tail strike on takeoff from Hong Kong's notoriously-difficult Kai-Tak airport.

Now, Taiwan Aviation Safety Council investigator Kay Yong has told reporters, "We have found… what we call multiple site fatigue cracks… with the length of nearly 70 inches," in the area of the patch, apparently caused by a poorly-engineered, or poorly-installed patch.

Decades of inspections, also, apparently failed to catch the now-nearly-six-foot cracks, surrounded by areas of corrosion, casting another cloud over the much-maligned Chinese maintenance workers at the state-owned airline.

The 747-200, one of a fleet of 30 that the airline owned at the time, was piloted by experienced crewmen; it was not long after the flight that pilot error was discounted as the cause of the disaster.

As we reported in May of 2002, the pilot was, "…Mr. Ching-Fong Yi with 6128 flight hours. The co-pilot was Mr. Yea Shyong Shieh with 6244 flight hours and flight engineer Mr. Sen Kuo Chao [had] 18024 flight hours."

It was not until recently, however, that evidence of just why the airplane fell out the sky was being made public.

FMI: www.china-airlines.com

Advertisement

More News

ANN's Daily Aero-Term (05.07.24): Hazardous Weather Information

Hazardous Weather Information Summary of significant meteorological information (SIGMET/WS), convective significant meteorological information (convective SIGMET/WST), urgent pilot>[...]

ANN's Daily Aero-Linx (05.07.24)

Aero Linx: The T-6 Racing Association The T-6 Racing Association is all about T-6‘s and racing. Our mission is to bring great racing to our fans in Reno and other venues wher>[...]

Airborne 05.01.24: WACO Kitchen, FAA Reauthorization, World Skydiving Day

Also: Electra Aero, AMO-CBP v Smugglers, Naval King Airs, Boeing Deal To the surprise of everyone involved, Waco Kitchen shut down both airport operations with little warning and h>[...]

Airborne Affordable Flyers 05.02.24: Bobby Bailey, SPRG Report Cards, Skydive!

Also: WACO Kitchen Bails, French SportPlane Mfr to FL, Dynon-Advance Flight Systems, Innovation Preview Bobby Bailey, a bit of a fixture in sport aviation circles for his work with>[...]

Airborne 05.03.24: Advanced Powerplant Solutions, PRA Runway Woes, Drone Racing

Also: Virgin Galactic, B-29 Doc to Allentown, Erickson Fire-Fighters Bought, FAA Reauthorization After dealing with a big letdown after the unexpected decision by Skyreach to disco>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC