NTSB: Downed Blimp Unable To Outrun Storm | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Recent Daily Episodes

Episode Date

Monday

Tuesday

Wednesday

Thursday

Friday

Airborne On ANN

Airborne 09.26.16

Airborne 09.27.16

Airborne 09.28.16

Airborne 09.29.16

Airborne 09.30.16

Airborne Hi-Def On YouTube

Airborne 09.26.16

Airborne 09.27.16

Airborne 09.28.16

Airborne 09.29.16

Airborne 09.30.16

Sun, Jul 10, 2005

NTSB: Downed Blimp Unable To Outrun Storm

Investigation Continues

The NTSB released the factual report this week about the crash of a Goodyear blimp in Coral Springs. The report quotes the pilot saying that the blimp was "unable to climb, make headway, or maintain directional control" with the engines at full power once caught in the storm.

The 192-foot-long gray, blue and yellow Stars and Stripes blimp crashed into an industrial park on June 16th after the pilot attempted to escape the storm.

The pilot had left the Pompano Beach Airpark about 1530 in good weather with scattered showers. He took the blimp south towards Miami Beach. About 1630, he started back for to the airport.

By 1725, the weather was worsening and showers were approaching the airport. While on approach, the pilot said that he saw several cloud-to-ground lightning strikes within a mile of the base. With the safety of the ground crew in mind, he decided to attempt to leave the area and wait out the storms.

Unfortunately, Mother Nature didn't cooperate, and the airship was "being pushed backward and down" even while the pilot was attempting to climb with full power. The heavy rain, lightning and "severe outflow and downdrafts" forced the aircraft down.

While the pilot attempted to steer away from homes, the blimp struck trees and powerlines while coming to rest top of a mini storage facility and several cars, vans, and trailers. The impact tore the helium-filled envelope and damaged the right propeller and lower fin of the craft.

The pilot, Daniel Thomas, 43, and passenger Charles Thomas, 48,were not injured.

FMI: www.goodyearblimp.com, www.ntsb.gov

Advertisement

More News

Missing PilotÂ’s Remains Bring Sister Closure After 51 Years

Mag. Dean Klenda Laid To Rest Sept. 17 Maj. Dean Klenda, an F-105 Thunderchief pilot, went to Vietnam in 1965. He never returned. His sister, Deanna, has been searching for answers>[...]

Airborne 09.30.16: ForeFlight/SiriusXM, FAA Takes On SMO, MH17 Shootdown

Also: Lynx Grounding, Drone Shooters, N Korean AirShow, Alaska Airlines, King Stallion, Embraer EMB 120, Pilot Arrested ForeFlight and SiriusXM have introduced SiriusXM Aviation we>[...]

Airborne 09.29.16: SpaceX Raptor, FAA v KSMO, First A330neo

Also: ISU Plane Mess, Redbird-NBAA-Deland, 1st Inuit Female Pilot, NTSB on Reno, Rotorwash, Air Tanzania Q400s, Av-Appreciation It looks like the concept of presidential candidates>[...]

Airborne 09.30.16: ForeFlight/SiriusXM, FAA Takes On SMO, MH17 Shootdown

Also: Lynx Grounding, Drone Shooters, N Korean AirShow, Alaska Airlines, King Stallion, Embraer EMB 120, Pilot Arrested ForeFlight and SiriusXM have introduced SiriusXM Aviation we>[...]

ANN's Daily Aero-Linx (10.01.16)

How To Make A Spaceship The story of the bullet-shaped SpaceShipOne, and the other teams in the hunt for the XPrize, is an extraordinary tale of making the impossible possible.>[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2016 Web Development & Design by Pauli Systems, LC