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Mon, Jun 15, 2009

Fuel Exhaustion Considered In Daytona Crash

Pilot Says He Thought Plenty Of Fuel Was On Board

The NTSB investigation of the May 25th crash of an Aero Commander (file photo, below) in Daytona Beach, Florida, which killed one person and injured the pilot, is focusing on whether the airplane had sufficient fuel on board. While the preliminary on-site investigation did not find sufficent fuel in the tanks of the airplane, or odor of fuel on inspection, pilot Andy Clark told the Daytona Beach news Journal he checked the fuel before flight, and thought he had about 110 gallons on board. The person killed was Clark's father, 80 year old Port Orange businessman Doug Clark.

A condensed version of the NTSB preliminary report follows:

NTSB Identification: ERA09FA303
14 CFR Part 91: General Aviation
Accident occurred Monday, May 25, 2009 in Daytona Beach, FL
Aircraft: AERO COMMANDER 500 S, registration: N73U
Injuries: 1 Fatal, 1 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

On May 25, 2009, at 0846 eastern daylight time, an Aero Commander 500S, N73U, operated by Commonwealth Aviation Corporation, was substantially damaged following a partial loss of engine power and collision with terrain, during a forced landing after takeoff from Daytona Beach International Airport (DAB), Daytona Beach, Florida. The certificated private pilot was seriously injured, and the pilot-rated passenger was killed. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight that departed about 0843, and was conducted under the provisions of 14 Code of Federal Regulations Part 91.

Preliminary information from the FAA revealed that the airplane was cleared for takeoff from runway 7R. About 1 minute after takeoff, the pilot reported "an engine failure" and announced his intention to return for landing on runway 25R. Witnesses in the vicinity of the airport, approximately 1/2 mile off the departure end of the runway, reported the engine noise from the accident airplane was "surging" as the airplane passed overhead, and one witness described a "radical" turn back to the airport.

Two witnesses, at their motorcycle repair shop, stated that only one engine was running. They added that the engine was "revving," and would then "conk out" before revving up again. As the engine surged, the airplane would "shuffle left and right." One witness described the airplane "just hanging there" as it turned back to the airport. The airplane flew west out of view before it crashed on the 1,000-foot grass safety area prior to the approach end of runway 25R.

A preliminary review of radar data revealed that the pilot declared the emergency when the accident airplane was leveling off at about 1,000 feet, about 1.75 miles from the departure end of the runway. During the turn back to the airport, the airplane descended to 700 feet, then climbed back to 1,100 feet. During the descent to the airport, the data showed the airplane at 93 knots, 700 feet and 1 mile from the runway, and 90 knots, at 500 feet and 1/2 mile from the runway.

A review of FAA and pilot records revealed that the pilot held a private pilot certificate, with ratings for airplane single-engine land, airplane single-engine sea, airplane multiengine land, and instrument airplane. His most recent FAA third-class medical certificate was issued on July 17, 2007. The pilot reported 1,250 total hours of flight experience on that date. Review of the pilot's logbook revealed approximately 1,470 total hours of flight experience; of which, 570 hours of which were in the same make and model as the accident airplane.

The airplane was examined at the site on May 25, 2009. There was no odor of fuel, and all major components were accounted for at the scene. The airplane came to rest on flat, grassy terrain on the airport property, 267 feet prior to the approach end of runway 7R. The wreckage path was oriented 240 degrees magnetic and was 140 feet in length. The airplane came to rest oriented 360 degrees.

The wreckage was removed from the site and the examination was resumed on the parking ramp on May 26, 2007. Examination of the cockpit revealed that the left and right fuel valve switches and the left and right fuel boost switches were in the "on" position.

The fuel system had a capacity of 226 gallons, was serviced through a single port on top of the left wing, and the tanks were interconnected to a center fuel sump that fed both engines. The fuel cells were opened through access panels and each were intact and contained only trace amounts of fuel. The airplane was leveled, the drain petcock was opened at the center fuel cell sump, and 1 quart of fuel was drained. The sample appeared clean, and contained trace amounts of sediment and water.

FMI: http://www.ntsb.gov/ntsb/brief.asp?ev_id=20090525X10534&key=1

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