USAF Rules Combination Of Factors Led To July F-15 Fatal | Aero-News Network
Aero-News Network
RSS icon RSS feed
podcast icon MP3 podcast
Subscribe Aero-News e-mail Newsletter Subscribe

Airborne Unlimited -- Most Recent Daily Episodes

Episode Date

Airborne-Monday

Airborne-Tuesday

Airborne-Wednesday Airborne-Thursday

Airborne-Friday

Airborne On YouTube

Airborne-Unlimited-04.01.24

Airborne-Unlimited-04.16.24

Airborne-FlightTraining-04.17.24 Airborne-Unlimited-04.11.24

Airborne-Unlimited-04.12.24

Join Us At 0900ET, Friday, 4/10, for the LIVE Morning Brief.
Watch It LIVE at
www.airborne-live.net

Tue, Nov 25, 2008

USAF Rules Combination Of Factors Led To July F-15 Fatal

Pilot Exceeded Limitation Speed, Entered Spin

A combination of human factors and aircraft anomalies caused a spin during a July 30 crash of a two-seat F-15D Eagle during a Red Flag exercise at Nellis Air Force Base, NV according to an Air Combat Command accident investigation board report released this week.

The pilot in command, Lt. Col. Thomas Bouley, was killed in the accident. An observer pilot, a Royal Air Force flight lieutenant, sustained minor injuries and was treated and released.

According to the AIB report, the accident pilot momentarily exceeded a technical order maneuvering limitation that is in place when the F-15D has fuel in the external wing tanks. Additionally, spatial disorientation resulting from the aircraft spin hampered recovery and was also cited as a cause.

When the pilot momentarily exceeded limitations, the aircraft departed from controlled flight due to the "left yaw/roll phenomenon," an aerodynamic anomaly that affects some F-15D's with two external fuel tanks. The departure, when coupled with an external wing tank fuel imbalance, resulted in the F-15 going into a spin.

Through simulations, investigators concluded that once in this spin, recovery was delayed by a radome, or nose cone, imperfection. Although the nose cone was too damaged to analyze, simulations provided substantial evidence that a radome anomaly aggravated the aircraft's spin recovery.

The violent and prolonged spin left the pilot spatially disoriented, which hampered the dive recovery, necessitating ejection. The observer pilot, who was sitting in the F-15's backseat, was ejected first, and he survived the crash. The mishap pilot was ejected .4 seconds later and did not survive the crash.

The aircraft, valued at $38 million, was assigned to the 57th Wing at Nellis.

FMI: www.af.mil

Advertisement

More News

ANN's Daily Aero-Linx (04.15.24)

Aero Linx: International Flying Farmers IFF is a not-for-profit organization started in 1944 by farmers who were also private pilots. We have members all across the United States a>[...]

Classic Aero-TV: 'No Other Options' -- The Israeli Air Force's Danny Shapira

From 2017 (YouTube Version): Remembrances Of An Israeli Air Force Test Pilot Early in 2016, ANN contributor Maxine Scheer traveled to Israel, where she had the opportunity to sit d>[...]

Aero-News: Quote of the Day (04.15.24)

"We renegotiated what our debt restructuring is on a lot of our debts, mostly with the family. Those debts are going to be converted into equity..." Source: Excerpts from a short v>[...]

Airborne 04.16.24: RV Update, Affordable Flying Expo, Diamond Lil

Also: B-29 Superfortress Reunion, FAA Wants Controllers, Spirit Airlines Pulls Back, Gogo Galileo Van's Aircraft posted a short video recapping the goings-on around their reorganiz>[...]

ANN's Daily Aero-Term (04.16.24): Chart Supplement US

Chart Supplement US A flight information publication designed for use with appropriate IFR or VFR charts which contains data on all airports, seaplane bases, and heliports open to >[...]

blog comments powered by Disqus



Advertisement

Advertisement

Podcasts

Advertisement

© 2007 - 2024 Web Development & Design by Pauli Systems, LC